When
This activity is done before the
refinement results is brought to
the painting section
Why
This delay activity is considered
ineffective because it takes a long
time, this activity occurs because
the operator stacking the
refinement results first before
being transported due to the
distance between the two remote
stations
How
Activity can be minimized by
closer the refinement station and
painting station where the
operational manager gives
direction to the operator so that
the refinement results can be
directly brought to the painting
station
3.1.9 Future State Map Depiction
Future State Map based on the results of proposed
improvements that have been made previously.
Changes in time included are changes in time that can
be observed or estimated from the current conditions,
while for the reduced time that can be obtained such
as a reduction of transport time and wood buildup due
to the reduction of activities that can cause waste at
the time of production. Future State Map can be seen
in Figure 5 below
Figure 5: Proposed Future State Map
3.1.10 Calculating Improved Process Cycle
Efficiency
The calculation of manufacturing lead time is done to
determine the condition of the original factory.
Calculation of Process Cycle Efficiency which
consists of manufacturing lead time calculation,
process cycle efficiency. The proposed
manufacturing lead time is 16352,76 seconds. The
calculation of process cycle efficiency is as follows
Process Cycle Efficiency
= 15151.76 / 16352.76 = 0.9266 ≈ 92.66 %
Efficiency increased = 92.66 % - 70.66 % = 22 %
Production Improvement =
Actual Manufacturing Lead Time - Proposed Manufacturing Lead Time
Actual Manufacturing Lead Time
(5)
=
21471.76 - 16352.76
21471.76
= 0.2384 x 177 = 42 units
4 CONCLUSIONS
Based on the analysis result using Lean
Manufacturing approach, the delay or non-value
added the activity that occurs during the production
process of wood making affects the productivity of
the company. This can be seen where after the
improvement with lean manufacturing approach there
is a change in manufacturing lead time which initially
equal to 21471.76 seconds become 16352.76 seconds.
Improvements to the Lean Manufacturing method
with improved results for Process Cycle Efficiency
increased by 22 % and for an average daily
production increase of 42 units to 219 units per day.
REFERENCES
Gaspersz, V, 2007. "Lean Six Sigma for Manufacturing and
Service Industry, PT. Gramedia Pustaka Utama,
Jakarta.
Liker, Jefrey K., 2006, The Toyota Way, Erlangga:
Indonesia.
Sundar, R., Balaji, A., & Kumar, R. S. 2014. A Review on
Lean Manufacturing Implementation Techniques.
Procedia Engineering 97, 1875-1885
Ali, Syed N. 2015. Productivity Improvement of a
Manufacturing Facility Using Systematic Layout
Planning
Haghani. 2015. A Genetic Algorithm For solving A Multi-
Floor Layout Design Model Of A Cellular
Manufacturing System With Alternative Process
routings And Flexible Configuration, Springer.
Das, B., Venkatadri, U., & Pandey, P. ((2014)). Applying
Lean Manufacturing System to Improving Productivity
of Coil Manufacturing. Int J Adv Manuf Tech, 307-323.
Wijayanto, Bagas, dkk. 2015. “Rancangan Proses Produksi
Untuk Mengurangi Pemborosan Dengan Penggunaan
Konsep Lean Manufacturing Di PT. Mizan Grafika
Sarana”. Bandung :Institut Teknologi Nasional
(ITENAS)
Sutalaksana, Iftikar, dkk. 2005. Teknik Perancangan Sistem
Kerja. Bandung: ITB.