Figure 9: Springback of a B pillar stamped by an
improved die.
From this figure above, we can recognize the
maximum springback value was +2.09mm and the
minimum was -2.82mm, which were largely reduced,
compared with the original springback values which
were +3.64mm and -5.21mm. Additionally, we also
can see most of the difference values locate in the
interval from -1.05mm to 1.05mm, the average
dimensional difference of these two models was
changed to be ±0.53mm, and the standard deviation
was 0.60mm; That was to say, all deviations were
reduced in some extent, so the analysis results
supported our improving work to be effective.
5 CONCLUSIONS
Taking a comprehensive survey on our whole work
in this paper, we introduced a systematic method to
reduce springback of a car B pillar, and we used
optical scanner, HandyScan 700, to obtain points
datum of a drawn B pillar, contrasting difference
between the points datum and primitive model in
Geomagic Qualify Probe to obtain springback values;
According to these springback values, we changed
die surface with a compensation value in CATIA;
Afterwards, we used DYNAFORM to simulate the
drawing process with the reconstructed die model,
and analysed the springback of the B pillar which
stamped with new die and punch whose surfaces
were compensated. The results confirmed that our
improving work to die was effective. This method
solves the problem which is difficult to predict and
measure the springback of a final sheet metal, so it
can be valuable in some engineering projects.
Because of the springback phenomenon, the
dimensional precision of a car B pillar is very
difficult to ensure; To obtain a qualified B pillar, the
traditional method to debug press tools mainly
depends on the experience of a bench worker. In that
case, the workload of the worker is very heavy;
moreover, it takes the worker enormous amount of
time to find where the press tools must be modified,
so that the traditional method lengthens the cycle of
press tools’ development and manufacturing. By
using our method introduced in this paper, we can
accurately find where the press tools should be
modified with a high efficiency, so it can shorten
press tools debugging cycle; Besides this, as the case
mentioned in this paper, we decreased the average
deviation value of the B pillar from 0.66mm to
0.53mm, so the results also satisfied us, thus it can
enhance the forming qualification and precision of a
sheet metal.
ACKNOWLEDGEMENTS
The authors gratefully acknowledge the financial
support of Guangxi Education Department Project
for Science and Technology, under project The
Precision Control Method Study for Whole Life
Cycle of a Die with reference KY2015ZL125.
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